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I have just installed the ERCF with ERB v1.1 board, flashed the RP2040 with newest klipper: mcu ercf(rp2040) Version: v0.11.0-241-gffb5105b Load: 0.00, Awake: 0.00, Freq: 12 MHz,
After I try to move with one of the motors, I always got this error (lines are from klippy.log):
`TMC gear_stepper failed to init: Unable to read tmc uart 'gear_stepper' register IFCNT
DEBUG: Found tmc2209 on gear_stepper. Current control enabled
DEBUG: Found tmc2209 on extruder. Current control enabled
I just updated and now have the same issue. Has anyone found a fix yet?
I ended up just throwing it out. Turns out there's a lot more wrong with the design than just the complete failure of the microcontroller. The on board power supply is under powered too, so there's no point in actually using this board.
Hi,
I have just installed the ERCF with ERB v1.1 board, flashed the RP2040 with newest klipper:
mcu ercf(rp2040) Version: v0.11.0-241-gffb5105b Load: 0.00, Awake: 0.00, Freq: 12 MHz,
After I try to move with one of the motors, I always got this error (lines are from klippy.log):
`TMC gear_stepper failed to init: Unable to read tmc uart 'gear_stepper' register IFCNT
klippy (1).zip
Is the wrong hardware or do I miss somethink else in the config?
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